Hey it is what it is right, can’t change anything now. I actually bought colder Ford performance plugs to switch them out because everything I read said I’d would need new plugs and they need to be gapped at .026-.028. I might still try and put one of the new plugs in cylinder 5 just to double check the shop gapped it right but leave them at the .030 they come at since I uninstalled the access port. All I can do is wait and hope/pray it’s just the injector. I’ve read nothing but good things about goose tune so figured I’d give it a try but I should of known better, I always have sh*t luck and random things happen to me. Thanks again for commenting, I appreciate it.That's just water vapor condensing in the exhaust, normal. I hate to say it, but having the misfire issue occur right after the tune was installed is pretty coincidental...